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A description
of the design, construction, and performance of a soil
vapor extraction system in response to the discovery
of the subsurface migration of methane-bearing LFG away
from a California landfill.
By
Stephen Ferry
The generation
of methane during the decomposition of waste buried
in landfills is a well-understood phenomenon for which
no practical means of prevention exists.
The lateral
migration through the subsurface of landfill gas (LFG)
containing as much as 50% methane by volume has been
documented at numerous landfill sites, including the
subject site. Often the preferential pathways of migration
are anthropogenic (such as gravel-filled utility easements)
and tend to conduct the gas directly to areas of human
activity (such as basement and ground-floor rooms of
nearby buildings). Because methane is combustible at
concentrations of more than 5% by volume, the uncontrolled
subsurface release of LFG has been recognized as an
immediate danger to life and limb in areas surrounding
landfills. Local enforcement agencies have formally
defined the conditions under which control measures
must be taken and the standards of performance that
constitute regulatory compliance. The regulations affect
virtually every landfill operating today.
This article
describes the design, construction, and performance
of a soil vapor extraction system in response to the
discovery of the subsurface migration of methane-bearing
LFG away from a landfill in California. A barrier to
gas migration approximately 6,000 ft. long, consisting
of 28 vertical gas extraction wells, was constructed
in two phases. The first phase was an eight-well pilot
system that was operated for approximately one year
to verify the theory that a unique design for the gas
control system would be appropriate for this site. The
second phase was a 20-well system incorporating the
design guidelines developed during the pilot phase.
Site Description
and History
The surface
topography in the vicinity of the landfill is flat,
and the native ground surface elevation is approximately
50 ft. above mean sea level (msl). The uppermost geologic
formation in the area, within which all project activities
were conducted, is composed of interbedded fluvial sands,
silts, and clays with inclusions of locally extensive
gravel lenses.
In the vicinity
of the project, the uppermost lithologic layer is a
deposit of silty clay approximately 25 ft. thick. Beneath
the silty clay lay an extensive 25-ft.-thick layer of
unconsolidated, poorly sorted stream-rounded cobbles
and minor amounts of coarse sand. Beneath the cobble
layer lay 70-80 ft. of interbedded medium- to fine-grain
sands, silts, and clays. This highly permeable cobble
layer, sandwiched between two lower-permeability zones,
formed an unusually extensive fluvial bedload deposit.
The extent of the cobble layer beneath the site was
definitively confirmed prior to the opening of the landfill
by gravel mining activities. The entire 100-ac. footprint
of the present landfill was mined by first removing
and stockpiling the upper 25 ft. of silty clay, then
removing and selling the underlying 25 ft. of cobbles.
The gravel mining operation at its conclusion exposed
a 25-ft.-high vertical wall of cobbles surrounding the
entire site, in the interval between approximately 25
ft. and 50 ft. msl.
After gravel
mining ceased, the stockpiled overburden was replaced
in the pit, filling it to approximately 28 ft. msl.
Figure 1 shows the landfill site in cross-section as
it existed immediately before the present landfilling
operation began. Prior to the deposit of the first buried
waste, the old gravel mining pit was reexcavated. All
of the redeposited overburden and an additional 15 vertical
ft. of the underlying dense, sandy silt were removed,
establishing the bottom of the landfill at an approximate
elevation of 15 ft. msl. Most of the waste accepted
since that time has been relatively inert construction
debris. When the LFG migration project was initiated,
approximately 1.25 million tons of waste were in place,
and the depth of buried waste was between 50 and 100
ft. over most of the 100-ac. extent of the landfill.
Pilot
Gas Control SystemModule 1
In response
to the first offsite detection of subsurface LFG, a
pilot gas control system (Module 1), consisting of five
monitoring wells and eight vapor extraction wells, was
constructed. Because it was known that the buried trash
had an unlined interface with the relatively permeable
cobble layer between approximate depths of 25 and 50
ft. below ground surface (bgs), it was suspected that
the cobble layer might be the primary pathway for offsite
gas migration. Module 1 was designed specifically to
test the theory that the primary pathway of gas migration
was through the cobble layer surrounding the landfill.
The first
step was to construct five triple-completion gas monitoring
wells. Each well consisted of three 0.5-in.-diameter
PVC pipes installed in a common 8-in.-diameter casing
and slotted at different intervals. In each monitoring
well, the deepest probe was slotted within the upper
part of the cobble layer. The shallowest probe was slotted
in the interval between 5 and 10 ft. bgs. The third
probe was installed with its slotted section midway
between the other two, approximately in the interval
between 15 and 20 ft. bgs. Each slotted interval was
isolated from the others by sand-cement bentonite grout.
The motivation
for installing triple-completion wells was to explore
the effect of the unique site geology on the pattern
of gas movement. The use of multiple monitoring zones
made it possible to observe the relative magnitude of
response, and the temporal sequence of responses, of
methane concentrations in the two subsurface facies
(cobbles and overlying silty clay) while gas extraction
activities were conducted nearby.
In response
to documented methane monitoring indicating that methane
was consistently present in three of the five monitoring
wells at concentrations greater than 5%, a row of eight
gas extraction wells on 225-ft. spacing was constructed
about 10 ft. from the perimeter of the landfill, which
was as close to the landfill property line as the drill
rig could work. The intent was to construct the wells
where they would intercept the undisturbed cobble layer
immediately outside the mass of buried waste, and in
fact all eight borings did encounter undisturbed cobbles.
The top of the cobble layer was encountered in each
boring at depths ranging from 22 to 31 ft. bgs, and
all extraction wells intercepted about 25 vertical ft.
of cobbles. All borings were terminated in the hard
sandy-silt native material below the cobbles at approximately
60 ft. bgs (the depth of the deepest buried waste) and
completed as vapor extraction wells to their full depth.
Although the potential exists for minor concentrations
of LFG to move downward within a soil profile as a result
of concentration gradient-driven diffusion, negligible
downward flux was expected because of the buoyancy of
methane (specific weight equal to 0.55 times that of
air) and the existence of the highly porous cobble layer.
Accordingly, no vapor extraction infrastructure was
installed deeper than the deepest buried waste.
The extraction
wells were constructed in 10-in.-diameter boreholes
drilled with a cable tool drilling rig. Well casings
of 4-in.-diameter Schedule (Sch.) 40 PVC were installed
in each borehole. Blank casing was installed from ground
surface to 5 ft. bgs, and factory-slotted (0.020-in.
slots spaced at eight slots per inch) casing was installed
from 5 ft. bgs to the borehole terminus. The borehole
annulus was filled with washed pea gravel opposite the
slotted casing intervals and with hydrated bentonite
pellets opposite the blank-casing intervals. The unusually
coarse filter pack was appropriate, given the large
average particle size of the target zone of remediation,
the cobble layer.
The placement
and construction of the extraction wells were different
from typical active gas-control system designs described
in the product literature. The placement of perimeter
extraction wells is usually in the waste itself, rather
than in native material immediately outside the waste.
This is because, at most landfills, the waste is more
permeable than the surrounding native subsurface. The
subject landfill, with its surrounding cobble stratum,
did not fit this characterization.
The design
of the extraction wells also differed from typical designs
described in the literature. The surface seals of gas
extraction wells are typically one-third to one-half
the depth of the well. For the pilot system, there was
a rationale behind installing wells with much shorter
surface seals and long, perforated intervals. For the
purposes of the pilot program, it was desirable to create
a sphere of extraction-well influence at the elevations
of all monitoring-well completions, not only at the
elevation of the deepest monitor probes (the probes
in the cobble layer). It was reasoned that if the monitor
probes in the cobbles responded faster and more strongly
than shallower monitor probes when gas was being withdrawn
from all elevations through the subsurface, the hypothesis
that the cobble layer was the primary pathway of gas
migration would be strongly supported.
Siting the
wells outside the waste offered other advantages besides
providing an opportunity to test the theory that extracting
gas from the cobble layer would be the most effective
way to mitigate offsite gas movement. Telescoping casings,
required where subsidence is a significant problem,
were avoided. Interference with, and gas system damage
resulting from, daily landfill operations was minimized.
Each wellhead
was provided with a sample port controlled by a 0.5-in.-diameter
ball valve; a 10-ft. section of straight, 2-in.-diameter
Sch. 40 PVC pipe with a 0.5-in. hole to accommodate
flow readings with a Pitot tube and differential pressure
gauge; and a 2-in. ball valve for flow control. Connections
from each well to the gas transfer header were made
with wire-reinforced flexible hose to accommodate movement
of the aboveground gas header in response to daily temperature
fluctuations.
The 2-in.-diameter
pipe in the extraction-well discharge piping was needed
to accommodate flow rate measurement with Pitot tubes
and differential pressure gauges because relatively
low gas flow rates were anticipated. Pitot tubes measure
two pressures inside the pipe: static pressure (which
acts equally in all directions) and total pressure (the
sum of static pressure and velocity pressure, which
acts in the direction of gas flow). Velocity pressure
is calculated as the difference between total and static
pressure, gas velocity is calculated as a function of
velocity pressure, and gas flow rate is calculated as
a function of velocity. In a 4-in. pipe, the flow rate
must be about 30 standard cubic feet per minute (scfm)
before velocity is great enough to create a total pressure
measurably different from the static pressure. By constricting
the gas flow path, velocity is increased and lower flows
can be measured. In a 2-in.-diameter pipe, flow rates
as small as about 7 scfm can be measured. Pitot tubes
cannot be used in pipes smaller than 2 in., the measuring
of flow rates inside 2-in. pipe employed the most accurate
method available within economic constraints.
The gas transfer
header to which each well was connected was made of
4-in.-diameter PVC pipe with a wall thickness of 0.075
in. and a standard dimension ratio (SDR) of 56. The
gas header was hung on the perimeter fence, and its
grade was established to trend toward two low spots,
where condensate was accumulated and released from the
gas transfer path via simple manometers (U-tubes with
a vertical height greater than the gauge vacuum inside
the pipe at the condensate release point). The gas transfer
header was connected to a small regenerative blower
with a capacity of 110 scfm and an applied vacuum of
20 in. of water column (WC) at the blower intake. The
relatively thin-walled thermoplastic pipe had adequate
collapse resistance to withstand this magnitude of vacuum,
even at summer temperatures of 110°F.
For the first
six months of operation (June to November 1992), the
gas flow rate from each extraction well was approximately
14 scfm and applied vacuum at the wellheads ranged from
0.1 to 0.7 in. WC. By November 1992, it was apparent
that offsite methane concentrations had more or less
stabilized at levels that were lower than preextraction
levels but still higher than 5% at most locations. It
was reasoned that increasing the flow rate per well
would result in more effective control of gas migration.
A focused extraction plan was developed to quantify
the extraction rate required to bring all monitoring
wells into compliance with the maximum 5% regulatory
mandate.
The focused
extraction procedure was directed at gas monitoring
well B (MW-B) and initiated on January 2, 1993. The
extraction rate at wells near MW-B were doubled to 27
scfm by closing the control valves of four distant extraction
wells and rebalancing the remaining nearby wells to
equal (increased) flows. On February 1, the extraction
rates near MW-B were further increased to 37 scfm by
closing one additional extraction well.
The results
of the focused extraction trial are illustrated in Figure
2. The figure shows how the methane concentrations observed
at MW-B decreased as the gas extraction rate employed
at the extraction wells closest to MW-B was increased.
The application of a 27-scfm-per-well pump rate for
one month did not bring the top zone of MW-B into compliance,
although a reduction from 11% to 7% methane was achieved.
When the pump rate was increased to 37 scfm per well,
methane concentration in the top zone of MW-B dropped
from 7% to 3% in less than two weeks. Methane in the
top zone of MW-B remained below 5% for the rest of this
focused extraction trial, which was concluded in mid-April.
It was concluded that a gas extraction rate of 37 scfm,
at an applied vacuum of 1-2 in. WC, was appropriate
for achieving compliance with extraction wells spaced
at 225 ft. at this site. Furthermore, the sequence of
responses of the three completions at MW-B was clearly
consistent with the hypothesis that the primary pathway
of subsurface gas circulation in the area of the landfill
was through the cobble layer. The lower monitor zone
responded first and most strongly to gas extraction,
and the top zone demonstrated the slowest and weakest
response to gas extraction, with the middle zone intermediate.
Main Gas
Control SystemModule 2
The design
of Module 2, situated along a different section of the
landfill perimeter where the same subsurface lithology
existed, incorporated the successful features of Module
1. A row of 20 gas extraction wells spaced at 200 ft.
was built in undisturbed native material, 10 ft. outside
the limit of the buried waste. The slotted interval
of each well was restricted to the cobble zone. A positive-displacement
blower capable of delivering 37 scfm per well was installed.
The design vacuum was a minimum of 10 in. WC at all
points in the gas collection header. The pipe schedules
used were Class 63 PVC (SDR 64) for all points in the
collection system where applied vacuum was expected
to be 50 in. WC or less; Sch. 40 PVC (SDR 24) where
applied vacuum was expected to be a maximum of 80 in.
WC; and Sch. 80 PVC (SDR 15) at the blower intake manifold,
where continuous vibration and an applied vacuum of
100 in. WC were anticipated.
Before construction
of Module 2, offsite gas monitoring wells were showing
methane concentrations between 35% and 45% by volume.
After 10 days of gas extraction, all wells had either
nondetectable methane levels or concentrations of less
than 5%.
Condensate
Handling
To collect
and treat condensate from the extracted gas, seven condensate
traps were situated at low points in the gas transfer
path, where the accumulation of condensate was anticipated.
Two sumps were placed at centralized locations to accumulate
the condensate collected from these traps and transfer
the condensate tinder pressure into the air-stripper
feed header. Wherever possible, condensate transfer
piping was configured to transmit collected condensate
by gravity flow. In some cases, collected condensate
was pumped back into the gas collection header in order
to transmit it to the closest sump without constructing
a separate line dedicated exclusively to condensate
transmission.
A key part
of the condensate collection system was a 6-in. electrically
actuated motor valve installed at the vacuum blower
assembly, on the suction side of the blower. The motor
valve was sized to accommodate the entire intake capacity
of the blower (8-in. inlet and discharge plumbing).
The motor valve periodically opens and thereby reduces
the vacuum applied to the gas collection system to zero.
The relief of applied vacuum allows condensate to be
released at various points throughout the gas collection
system so that collected condensate can flow by gravity
out of the gas header, through check valves, and into
traps. The timing of the operation of the motor valve
is controlled by a liquid level float switch in the
moisture knockout pot (KO pot), located at the blower
intake, where the rate of condensate accumulation was
expected to require the most frequent discharge.
The need
for periodic vacuum relief to facilitate the release
of collected condensate from the gas transfer path was
the result of the relatively high vacuum in the gas
header. The applied vacuum in the gas collection header
ranges from approximately 10 in. WC to 80 in. WC and
can be as high as 100 in. WC in the KO pot. For a condensate
trap to allow the continuous release (without vacuum
relief) of condensate from the gas header, while still
preserving the vacuum inside the gas header, a U-tube
arrangement with a height equal to the applied vacuum
would be required. The U-tube would have to be situated
entirely below the elevation of the invert of the gas
header, which in this case would have required numerous
facilities to be constructed between 6 and 8 ft. bgs.
The installation of numerous deep U-tubes was rejected
because of the required excavation.
Engineered
check valves, with cracking pressures precisely matched
to the line vacuum at the trap location, were considered
as an option to reduce required excavation depths. They
were rejected because the line vacuum changes daily
as a result of changes in barometric pressure, changes
in well-field configuration or well flows, and changes
in the condition of the ground-surface seal around the
extraction wells. The dependable operation of engineered
check valves could not be guaranteed in an application
for which the required cracking pressure was not constant
from day to day.
The cost-effective
solution to the problem of releasing condensate from
high-vacuum sections of the gas header was to periodically
reduce the applied vacuum to zero, permitting the drainage
of condensate through shallow U-tubes incorporating
standard zero-cracking-pressure check valves. The check
valves were installed in an orientation in which they
would be opened by the weight of the collected water
upon relief of vacuum and would be closed by atmospheric
pressure upon reestablishment of vacuum.
Guest
author Stephen Ferry is a consulting engineer based
in Napa, CA.
MSW
- July/August 2002
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